Publication Date:
2019-06-28
Description:
This paper describes the results of a program initiated to identify the cause and the mechanism of 4-kHz vibrations of the Space Shuttle main engine's (SSME's) LOX inlet tee, which were revealed in 17 percent of the SSMEs during ground tests. The results of the engines' inspection, structural analyses, computational fluid dynamics studies, literature reviews, expert consultations, and laboratory testings identified the probable cause of the 4-kHz vibrations being related to the fact that the walls of some tees were thinner than in the mojority of tees, resulting in less stiff structures. The mechanism of the vibrations was identified as vortex shedding in combination with a structural coupling with the thrust cone, which increased the vane mobility, which, in turn, aggravated the fluid coupling with the thrust cone. As a result, the vane mobility was increased, aggravating the fluid coupling with the vanes. An internal modification was developed and was successfully demonstrated on an engine that had previously exhibited a 4-kHz problem.
Keywords:
GROUND SUPPORT SYSTEMS AND FACILITIES (SPACE)
Type:
AIAA PAPER 88-3132
Format:
text
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