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  • Aircraft Stability and Control  (2)
  • AERODYNAMICS  (1)
  • Chemical Engineering
  • General Chemistry
  • unknown
  • 1965-1969
  • 1945-1949  (3)
  • 1947  (3)
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  • 1965-1969
  • 1945-1949  (3)
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  • 1
    facet.materialart.
    Unbekannt
    In:  CASI
    Publikationsdatum: 2016-06-07
    Schlagwort(e): AERODYNAMICS
    Materialart: NACA Conf. on Aerodyn. Probl. of Transonic Airplane Design; p 15-20
    Format: application/pdf
    Standort Signatur Erwartet Verfügbarkeit
    BibTip Andere fanden auch interessant ...
  • 2
    Publikationsdatum: 2019-07-11
    Beschreibung: At the request of the Air Materiel Command, Army Air Forces, an investigation of the low-speed, power-off, stability and control characteristics of the McDonnell XP-85 airplane has been conducted in the Langley free-flight tunnel. The results of the portion of the investigation consisting of tests of a 1/10-scale model to study the stability of the XP-85 when attached to the trapeze and during retraction into the B-36 bomb bay are presented herein. In the power-off condition the stability was satisfactory with all oscillations well damped and the nose-restraining collar could be placed in position without difficulty. In a simulated power-on condition the model had a constant-amplitude rolling and sidewise motion and when the collar was layered, a violent motion resulted if the collar struck the model but failed to hold it in the proper manner. Folding of the wings and retraction into the bomb bay offered no problem once the airplane was properly held by the collar. It is recommended that the power be cut immediately after hooking on and that a restricting mechanism be incorporated in the center of the trapeze to eliminate the sidewise motion. It also appears desirable to have the retracting procedure controlled by the XP-85 pilot or an observer in the mother ship to insure that the parasite is in proper position after hooking up before bringing the collar down.
    Schlagwort(e): Aircraft Stability and Control
    Materialart: NACA-RM-L7J16
    Format: application/pdf
    Standort Signatur Erwartet Verfügbarkeit
    BibTip Andere fanden auch interessant ...
  • 3
    Publikationsdatum: 2019-07-12
    Beschreibung: Attempts were made to alleviate the buffeting of external fuel tanks mounted under the wings of a twin-engine Navy fighter airplane. The Mach number at which buffeting began was increased from 0,529 to 0.640 by streamlining the sway braces and by increasing the lateral rigidity of the sway brace system. Further increase of the Mach number, at which buffeting began to 0.725, was obtained by moving the external fuel tank to a position under the fuselage.
    Schlagwort(e): Aircraft Stability and Control
    Materialart: NACA-RM-SA7A07
    Format: application/pdf
    Standort Signatur Erwartet Verfügbarkeit
    BibTip Andere fanden auch interessant ...
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